Tuesday, August 22, 2017

Adventures on the Chesapeake - Part Two

Captain Mike approached Rosalind on the starboard side and put out the towboat's large fenders. He asked, "Are you guys safe?" We relayed that everything was fine. He said, "There is a boat that has gone ashore on the beach at Chesapeake Beach. Do you mind if I take care of her first?" We told him that we were fine and that we would be standing by. He thanked us and headed south. Within a few minutes, he was barely a speck on the horizon. Then, the speck started getting larger again. The towboat was back in less than 10 minutes. Someone else had been able to help that boat in distress on the beach.

Now at Rosalind, Captain Mike handed me a bridle attached to the 2 inch (50 mm) diameter hawser, which would be used to tow us.  I ran the bridle lines through the fairleads at the bow and attached them to the bollard. With Cheryl at the helm and me at the bow, he payed out the hawser. We had readied the windlass and started pulling up the anchor chain with the windlass remote. Captain Mike was slowly moving the towboat forward and when Rosalind's anchor chain was almost taut, and without any prompting, he said, "Let me give you a short pull to get your anchor free." With the anchor free, it took but a minute to get the remaining 18 ft (5.5 m) of chain on board. With the anchor on the bow roller, the only thing left to do was to move the bridle over the anchor so that when the towboat pulled us, the anchor would not be forced up on the roller and hit the boat.

With the bridle sorted and the hawser taut, I went aft and took the helm. The towboat headed west and we followed, picking up speed to 6 knots (11 km/h).


Rosalind being pulled along in Herring Bay

In less than fifteen minutes, we passed the Herring Bay Light Red 2 at the south end of Herring Bay. There is a shoal spit from the marker all the way to the northern end of Herring Bay. The depth sounder momentarily registered 5.5 feet (1.7 m) as we rounded the mark. Our depth sounder is to port and with the shoal to starboard, we had less than 6 inches (15 cm) of water under our keel. We informed the Captain and he made a slight course correction. Twenty minutes later, we were slowing down. We were just outside the breakwater at Tracy's Landing. I released the bridle from the bollard, Captain Mike flaked the hawser in the towboat and came alongside Rosalind. We were securing the towboat on Rosalind's aft starboard quarter when a 50 ft (15 m) powerboat came off a plane within a boat length from us. Its wake caused Rosalind and the towboat to bang together violently. Luckily, the fenders did their job and neither boat or our suspended dinghy got damaged. The Captain aptly said, "Some people just think about themselves..." We got Rosalind and the towboat tied together and we started moving forward. I turned the wheel to starboard and the Captain picked up the slack on the forward line holding both boats together. Doing barely 3 knots (5.5 km/h), we passed the breakwater and entered the channel. A 40 ft (12 m) fiberglass sloop was a little over 50 ft (15 m) in front of us. Going over the entrance, the depth sounder registered 5.5 then 5.3 then 5.1 ft (1.7 then 1.6 then 1.55 m). No much to do other than push on. The depth sounder dropped to 4.9 ft (1.5 m).  We barely had an inch (2.5 cm) of water under our keel! Then, we were over the sandbar and in deeper water. I called the marina and informed them of our location.

Rosalind entering Tracy's Landing

The marina was going to send a dockhand to help us get Rosalind in her slip. I shared the slip location information with Captain Mike and a couple of minutes later we were slowing down and turning to port into the fairway between docks G and H. Cheryl had prepared and positioned our docking lines and Captain Mike eased us into slip H8. Rosalind rested in the middle of the slip, without having touched the dock or any of the pilings. Captain Mike is a true pro! We secured Rosalind in her slip and went to grab a lunch.


Rosalind gently placed in slip

The next day, we went on board and took care of the fuel system. We drained fuel from both tanks and confirmed that there was no more water in either tank. We also made sure no water had entered the engine through the engine exhaust system from the waves slamming our stern when we were at anchor. Everything was fine. We started the engine and let her run for 40 minutes. Rosalind was now ready to be hauled.

Thank you for following along,
Alex and Cheryl


Tuesday, August 15, 2017

Adventures on the Chesapeake - Part One

On Sunday, August 13 we left Galesville and started heading South. The day trip was supposed to be a short 4-hour motorsail between Pirates Cove on the West River and Herrington Harbour North Marina in Herring Bay. The plan was to haul Rosalind, do some work minor work on the rudder, install the satellite communication antenna on the mizzen mast, and paint the bottom before continuing South.

The weather forecast called for 5 to 10 knots of wind from the North. We left our mooring at Hartge Yacht Harbor at 8 am and by 8:20 we had the jib out and were motorsailing out of the West River doing 4.8 knots. We cleared the Green Can 1 and headed east to avoid the shoal on the south side of the river entrance extending out one and a half miles (2.5 km) to the north, northeast past Curtis Point. The wind picked up to 12 to 14 knots when we got in the Bay and the two-foot (60 cm) short waves gave Rosalind a rocking but pleasant motion. A little over half an hour later we pointed Rosalind south and headed towards Herring Bay. The apparent wind dropped and we decided to put up some more sail in order to take advantage of the following wind. Cheryl uncovered the mizzen and then took over at the helm and I went to the stern deck to raise the mizzen. I had just finished raising the mizzen when, from the direction of the cockpit, a buzzing sound told me something was amiss. Cheryl called out from the helm, "The Racor Water Alarm just came on!" I got to the cockpit, throttled back Lucy, our trusted Beta 30 diesel engine, and pulled the engine stop lever. We were heading south with a northerly wind and 20 feet (6 m) of water under our keel. Cheryl stayed at the helm and I went down the main cabin, removed the companionway stairs, got a flashlight, and opened the engine room access hatch. The Racor bowl was half full with water.  The alarms panel had earned its keep again!

Racor Alarm Lit-up (Red Light in Lower Left)

We had 10 nautical miles (18.5 km) before we had to turn north before entering Herrington Harbour North. First things first:  Get the water out and start up Lucy again.  In order to drain the Racor fuel water separator, I had to crack the T-handle at the top of the filter enclosure in order to break the vacuum. I drained about a cup of water from the Racor and retightened the T-handle. The alarm light turned off. Just to be sure that all the water was out, I went to aft cabin and got a piece of spare hose, got the five gallon (20 liter) empty diesel gerry can from the starboard lazarette, and using the diesel hand primer bulb (which I installed when we replaced the engine last year), I connected the hose to the bottom of the Racor, and got about a gallon (4 liters) of diesel out of the starboard tank.

It was time to start the engine again. Lucy fired up and after less than a minute, Lucy stalled! What happened? After removing the water, I neglected to refill the Racor with diesel. (Diesel engines do not like air in the fuel. Air locks up the high pressure pump, no fuel can get though, and the engine stalls). Nine miles (16.5 km) to go to the south end of Herring Bay...

We sailed south southwest for an hour and we were in some calmer waters. With the sails still pulling us along, Cheryl stood on the port side of the cockpit and navigated and steered Rosalind. I opened the engine room, got in the main cabin and removed the air from (bled) the engine. I had to do this twice to get all the air out of the Racor, fuel lines, lift pump, fuel filter, and high pressure pump. Lucy started right up and ran smoothly. Ten minutes later, the Racor alarm buzzed again! We shut her down and keep sailing. I went below and looked at the Racor bowl. The red-colored diesel should have been clear but it was not. Its cloudiness was an indication that there was some water still present.

We decided to sail to the south end of Herring Bay, still 6 nautical miles (11 km) away, and then anchor. After a couple of hours, we furled the jib, Cheryl turned Rosalind into the wind, and I dropped anchor. It was clear that it would take some time for the water to separate from the diesel and settle down to the bottom go the Racor. We now had two choices:  We could launch our dinghy and with our three horsepower outboard engine push Rosalind for the last five miles (9 km), or get a tow. We have used our dinghy as a push tug in the past and this can work well. The only two limitations are that you have limited maneuverability (because you have limited horsepower) and its best done in calm waters.

The entrance to Herrington Harbour North is at the top of a narrow channel. The four mile (7.5 km) channel is too narrow to tack in and the wind was on the nose. Once you get to the entrance, you must navigate between markers over a sandbar. There is a shoal in the middle of the creek and the marina fairways are very narrow. Additionally, when the weather is fine, the entrance can be very crowded with boats leaving and returning to the marina simultaneously. After a short discussion, we opted for the tow. We made the call. While waiting, I opened the starboard fuel tank deck fill and Voila, the o-ring that was supposed to act as a seal to prevent water from entering the tank had split and there was a clearly visible 1/2 inch (12 mm) gap.

Failed O-Ring from Diesel Filler Cap

Starboard Diesel Filler Station Taped to Prevent Further Water Intrusion.

Captain Mike, running the towboat, called us on the cellphone and we shared our coordinates. He was 1.9 miles (3.5 km) away...

Wednesday, August 9, 2017

Replacing the old Perkins 4-108 Diesel Engine

The Perkins 4-108 diesel engine that was on Rosalind when we purchased her was a 1984 vintage engine that was in serious need of a rebuild or replacement. While the engine ran well, the engine mounts needed to be replaced and there were indications of corrosion on the high pressure fuel lines. One fuel line had started leaking and we replaced it shortly after we got Rosalind. Additionally, we replaced the Racor fuel-water separator and sorted out the fuel system. The engine ran well, started easily enough and it did not burn oil, but we knew that spare parts were getting hard to find and we also knew that water had found its way in the fuel system, possibly corroding the very expensive high pressure diesel fuel pump.

So after estimating that it would cost just about as much to rebuild/refurbish as to get a new engine, we opted for the new engine. The first question was determining what engines would fit in the engine room and how large of an engine we really needed. Looking at the numbers, we quickly realized that the engine size was really driven by the size of the propeller aperture in the hull. The propeller aperture dictates the largest propeller that can be used on the boat and the propeller size specifies the maximum horsepower that can be delivered in the water from the engine. So, we measured the aperture, calculated the maximum propeller size, determined the type of propeller (three bladed with large surface area), and identified the maximum horsepower. We then started looking at gearboxes and engine horsepower curves and identified the Beta 30 hP engine as a good match for our needs.

The Perkins was rated at 42 hP but we were going for 30 hP, were we concerned? Looking at the engine-gearbox-propeller combination, we found out that we could not effectively use anything much more than about 28 hP, as the propeller would start caveating and loose thrust efficiency. So while we "had" 42 hP, we never used them all, so we opted for an engine that was better matched to the hull length and hull propeller aperture and went with the 30 hP.

We chose the Beta 30. There was another major advantage to the 30 hP engine. By going from a four cylinder to a three cylinder engine, we were able to move the engine-gearbox forward in the engine room. After (very) careful measurements, we were able to place the engine so that the transmission (gearbox) could be removed for service without having to disconnect the engine. This is a major benefit as gearboxes can fail more frequently than engines. On our previous boat, we did not have that option and both times we had the gearbox rebuilt, we had to remove the entire engine in order to remove the gearbox. Additionally, the new engine-gearbox location enabled the shaft coupling to move forward in the engine room and this makes it accessible for precise engine alignments.

Sea trials confirmed that we indeed had plenty of power and that any larger engine would have only added weight and limited access in the engine room.

The engine replacement process was complex and multifaceted. We had to work in 3D and locate the engine in the engine room with tolerances of only thousandths of an inch (hundredths of a millimeter). The main steps involved with the engine replacement were the following:

1. Document the old Perkins engine installation, including labeling of wiring and hoses.
2. Place order for new engine with custom engine feet matching the dimensions of old engine.
3. Disconnect old engine.
4. Suspend and relocate old engine in order to remove old gearbox.
5. Disconnect gearbox from old engine.
6. Hire crane to remove old engine.
7. Refurbish engine room (including replacing all 40-year-old through hulls and hoses).
8. Replace cutlass bearing.
9. Measure, order, and install new shaft and propeller.
10. Hire crane to install new engine.
11. Install instruments panel for new engine.
12. Customize engine exhaust riser (welding stainless steel done by welder)
13. Connect engine exhaust, fuel, water, remote oil filter and electrics.
14. Align engine.
15. Commission engine and conduct sea trials.

The replacement of the old cutlass bearing was challenging as we had no information as to how to disassemble the old bronze fixture. The other big challenge was the engine alignment. What we found after having the new engine placed in the engine room was that the old engine was improperly placed in the engine room (with respect to the shaft) and therefore the custom engine mounts of the new engine were off by 3/4 of an inch (1.8 cm).  In order to remedy this problem, we reworked the engine stringers and ended up with the engine in the correct location. When all was said and done, this took the better part of six to seven weeks to resolve.

After some initial sea trials last fall, we sorted out some engine mount and exhaust issues that we wrote about last fall. We are very pleased with the new engine and already have put 90 hours on it. Here are some pictures of the engine removal and installation process. We hope you enjoy.

Alex and Cheryl

Old Perkins 4-108 Engine

 Old Engine Suspended in Order to Remove Old Gearbox
(necessary in order to be able to remove the engine through the hatch opening)

 Engine Disconnected, Gearbox Removed, and Cockpit Padded Prior to Engine Removal

 Old Engine (without gearbox) Hoisted by Crane

Rusted Old Engine Mounts 
(Mounts had failed and were no longer providing proper engine support)

 Engine Room After Removal of Old Engine (yuck!)

 Removal of Old Propeller and Shaft

 Disassembly of Cutlass Bearing Holder

 New Propeller, Cutlass Bearing, and Shaft Installed

Working on Adjusting/Lowering the Engine Stringers - Note Void next to Blue Tape 

Port Stringer Re-fiberglassed


 Refurbished Engine Room with Relocated Stringers and New Engine Mounts

Preparing for the Installation of the New Instruments Panel

New Instruments Panel Installed - Cockpit Port Side


New Beta 30 Engine Installed!

Tuesday, August 1, 2017

The New Alarms Panel - It works!!!

When we re-engined, we repurposed the old engine instrument panel to house various gages, switches and alarms to create an Alarms Panel. 

Old Engine Instruments Panel - Instruments removed

New Alarms Panel

The new Alarms Panel houses the Racor Vacuum gage, in the upper left, to let us know when the diesel filter is clogging up and the Racor water sensor alarm, in the lower left to let us know if water finds its way into the diesel. A clogged filter and/or water in the diesel will stall the engine, and water in the diesel will also cause damage to the engine. The panel also houses the anchor windlass Up/Down switch, in the upper part of the panel, and an digital ammeter, in the upper right, to let us know how hard the windlass is working. This is important as we do not want to burn out our new windlass motor and have to raise the anchor and chain by hand! Lastly, the panel lets us know if there is any water in the aft or engine room bilge. If there is water in one of the bilges, an alarm will sound and an LED light will let us know which bilge has the water. By depressing the switch (the switches have built in LED lights) we can silence the alarm; however, the LED will remain lit as long as the bilge pump is dewatering. In the middle of the panel there is an insulated cup holder (it fit perfectly in the old tachometer hole!). We use it to store pens, a grease pencil (handy on waterproof charts), and magic markers.  

On Rosalind, we have the option to divert the cockpit drains overboard or into the aft bilge. In the event the cockpit fills with water, the boat will sit lower on the water due to the extra water weight and this could potentially submerge the drains. If that is the case, the cockpit will not drain and water could start filling the boat! As a precaution/remedy, we can divert the water to the aft bilge and safely remove it with various pumps.

Over the winter I rewired the aft bilge pump, connected it to our Alarms Panel, and installed a new float switch to replace the old one. We now have a selector switch in the aft cabin to let us turn on the pump manually or connect it to the new float switch which automatically activates the pump when there is any water in the aft bilge. 

Aft Cabin, Looking Aft - Bilge Pump Auto/Manual Selector Switch (in black) Located on Starboard Side above Yellow Life Raft

During spring commissioning, before we moved onboard, we got a call from the Harbormaster at Hartge Yacht Harbor where Rosalind is moored. Our bilge alarm for the aft bilge was buzzing. The Harbormaster heard the alarm from shore and used his launch to inspect Rosalind  All was well. There was no water finding its way onboard, but there was just a little water in the bilge. We immediately drove to the marina and got onboard to figure out what happened. We found that we had left the cockpit drain valves to the bilge position. We had also removed the sides of the cockpit enclosure and as a result, some water got in the cockpit from a strong thunderstorm that passed through Galesville.  The pump worked, the alarm system worked, and even the new float switch worked perfectly. I had just installed the new float switch 1/2 inch (1 cm) too low, and the pump could not get the last bit of water out of the bilge! It took but a minute to re-adjust the pump switch elevation. 

I have always wanted to install an alarms panel and I am very happy that we have one on Rosalind.  When putting it all together, a year ago, I remember testing the buzzer at home and thinking, "Boy, this is loud!" That loudness sure came in handy!  It took eight coats of varnish and lots of work to wire it all but in the end it was all well worth it!

Thanks for visiting,
Alex and Cheryl